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solgt

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Posts posted by solgt

  1. Okay last update for the turbo overboost issue :l....

    So when they had it off the car and were looking to see if swapping housings was possible (which i learned after wouldn't be from lots of really good info on Jack's soap opera thread haha), they gave me a call and the guys said there's a crack in the housing which is causing the wastegate to not open essentially. I don't know how something like that can happen especially if BNR truly took it apart and made sure everything was in spec. So my theories: either it was cracked from Jack or maybe started there which could have been giving him his boost issues which was solved atleast for a little while with upgraded springs/porting, or BNR never really took it apart to make sure everything was good..or he noticed but decided not to do anything about it. Sooo I guess that's how my week is going, expensive ass paper weight :[

     

    They got my stock turbo back on the car, finished up doing the last of the wiring for my headlights (halos/demon eyes and putting in a fog light switch since they were right there) and my tuner said that he was just going to try getting me into a tuning slot as soon as possible. Hopefully that takes care of my small little soap opera of problems for a while and the downpipe doesn't end up giving me any problems, will update again when its tuning time

    Dam son. That's really fubar. At least you have a stock unit to get going.

    Is it possible that since you have it, it has cracked? Lord knows. As you said it may have started from 1 and not noticeable until you. Or it just cracked from your use. Going from one location, temp, humidity, elevation plus cold/heat cycles to another may play a role. I'm just playing devils advocate to offer other ideas. Cause dam that-really-sucks. Expensive paper weight.

     

    Hope the tuning goes well and last!

  2. I rather not trailblaze to see what is the actual limit of trans and diff is.

    Today must've had some thing in the water cause I got hit today by a guy in a Corolla who swerved into my lane without checking first. Instead of slowing down for the suv in front of him making a right. Then tried to evade me. In. A stock. 10' Corolla. FML!!!!!! Tried to say it was my fault cause I was speeding. I mean his rear driver door was at my front passenger door and he swerved into me. In a group of 5 cars he swerved hits my front right with his back left and say I was speeding. Wow. I mean WOW. Good thing for and Hawk brake pads and USAA

  3. Yes yes....what turbo is it??!! I'm just holding off until I can get a final tune with an proper intake

    I've vastly improved the intake so that's a less limiting factor. Now from my readings on the forums the RacerX is just the step over stock when compared to the KillerB unit. So that's the next step. I know I'm basically at the theoretical threshold of driveline components outside of the clutch so I'm not really wanting to push it that far(lol) as this is my daily.

  4. Whoa... you going FlexFuel? Did your tuner limit torque to 350 because of the tranny? [emoji38]

    I'm really interested in Cobbs new device although I'm sure t00ning is uber critical. Maybe after a tmic upgrade. Insufficient air supply was the limiting factor of the power. Thus working on intake. And yes I'm kinda worried about blowing a gear or the whole trans. Knock on wood.

  5. http://legacygt.com/forums/attachment.php?attachmentid=227856&stc=1&d=1459998989

     

    Block out

    http://legacygt.com/forums/attachment.php?attachmentid=227857&stc=1&d=1459999080

     

    Pistons

     

    http://legacygt.com/forums/attachment.php?attachmentid=227858&stc=1&d=1459999080

    AndrewTech

    http://legacygt.com/forums/attachment.php?attachmentid=227859&stc=1&d=1459999080

     

    Getting food today. NOM NOM NOM NOM

    1481126397_blockout.thumb.jpg.45dd317d660c5cf6cd7f0f47e9afb8f9.jpg

    pistons1.thumb.jpg.5493b7a8a5f30b7718ef8fa1183bebcc.jpg

    20120817_161440.thumb.jpg.a39319062262804127ba9ca559fec51c.jpg

    IMAG3114.thumb.jpg.a372f2e65a41a1fd4037c7a4cc46712f.jpg

  6. Few pics.

     

    New turbo from BNR

    http://legacygt.com/forums/attachment.php?attachmentid=227485&stc=1&d=1459467497

    Fresh pistions installed

    http://legacygt.com/forums/attachment.php?attachmentid=227486&stc=1&d=1459472060

    New look engine bay kinda dirty

    http://legacygt.com/forums/attachment.php?attachmentid=227487&stc=1&d=1459472060

    That bov is loud!

    http://legacygt.com/forums/attachment.php?attachmentid=227488&stc=1&d=1459472060

     

    Dyno vid to follow soon;-)

    IMAG2900.thumb.jpg.7e1ab4cb77a15425e7f641c70e86b3a9.jpg

    20150914_170210.thumb.jpg.124c15bab75fefff8f01117de9b892c0.jpg

    IMAG2910.thumb.jpg.7f9eef3bd30efbf5d5ecbdf53a6b05c2.jpg

    IMAG2911.thumb.jpg.081ac9a0a0d709ad67ae69d7d251ea51.jpg

  7. After about 3yrs of and modding figured I'll share.

    I drove it stock for a couple months. Flashed the Cobb ots 93 before going further for S&G to see if it really made a difference and suprise! It was. A very welcome one at that.

     

    Part 1.

     

    Suspension:

     

    Tein 2" springs

    WhitelineL 22mm front 2way lower sway

    WhitelineL 22mm rear 3way lower sway

    WhitelineL f/r endlinks

     

    Engine:

     

    Invidia turbo back

    Cobb Ap

    K&N panel filter

    Resonator delete

    Perrin 3 port bcs

    Grimm ebcs

    TurboXS recirc bov

     

    Made 247whp@6200\330lb-ft tq@4300 @19-20psi by Jermaine@turboxs

     

    Intermission

     

    Worked great till stock tmic end tanks let go. Thus call was placed to Brian at racerx and his tmic was sent out. His charge pipe wasn't available at the time. Still in development phases.

     

    Part 2.

     

    Then head gaskets started leaking and build began.

     

    Sam and Riyaad, Jacob and of course the guru himself Andrew, deserve HUGE Thanks for making this possible!

    With the engine out, heads off, inspection was scrutinized for warping of heads or any other possible major worries. None found so progress insued!

     

    Racing water pump

    Timing belt

    1000cc ID inj

    300lph fuel pump

    08 sti oil pump

    ARP headstuds

    Weisco Pistons

    Engine gasket kit

    BNR HTA-71 20G ported turbine\ compressor housings and wastegate

    RacerX charge pipe

    Crawford air\oil seperator

    Perrin tmic coupler

    Perrin shifter bushing

    Clutch damper delete

    TurboXS rfl bov

    Custom Cobb SF intake

    Garageline.com 20mm wheel spacers

     

    Tuned again by Jermaine

    350hp\350tq@ 23psi.

     

     

     

    So other than the exhaust led marker lights and license plate brackets from AndrewTech nothing cosmetic has yet been done the car.

     

    The BIGGEST THANKS go to the wife for not killing me for building it while she was pregnant!

     

    Thanks guys for reading. I'll post pics and dyno video later

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