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solgt

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Posts posted by solgt

  1. Was it something you wanted to try out?

    What is the purpose of the resonator?

    Did it increases your airintake?

     

    Sent from my SAMSUNG-SM-G925A using Tapatalk

    This is my factory airairbox looking at it from the bottom. Front facing away. The resonator blocks this opening and reduces that diameter at the bottom of said resonator to a 1-2mm opening. To me that's free horsepower. Definitely not enough to tune for but does allow more airflow to filter. Literally the 1st mod I did.

     

    http://uploads.tapatalk-cdn.com/20160906/b5c4c6a60ea7e474255cce6b1c79b571.jpg

  2. Invidia turbo back

    Suspension and exhaust install by Andrewtech Automotive

     

    K&N drop in panel filter

    Intake resonator removed

    Cobb Ap

     

    Tuned to 247whp@6200\330lb-ft tq@4300 @19-20psi by Jermaine@turboxs

     

    While there a Perrin 3port bcs and turboxs recirc bov was added

    Everything else stock.

     

    Worked great till stock tmic end tanks let go then a call was placed to Brian at racerx and his tmic was sent out. His charge pipe wasn't available at the time. Still in development phases.

     

    Then head gaskets started leaking and build began.

     

    FMIC FTW will be next.

    I'll organise op to better show my progression soon. Hope this helps.

  3. Nice build! Stage 2 didn't really feel that much different from stage 1?

    Mind you I went 2in drop, which to me makes more power translate to the operator over stock ride height. But will say driving around town the torque available to use doesn't change a great deal. On the highway, yeah full pull 2-3-part 4 you will. Given that until the turbo or motor is changed the result will be the same. Great torque, not much horsepower. Which given my experience with cooling needs, going stage 2 in my opinion dutifully needs cooling added to list for longevity of components. I havnet gotten a radiator yet. Been on the fence on Mishimoto or Koyo and truly have been slaking. Huge fan of adding an oil and trans radiator in place of top mount when I go front mount. Thouhts?

  4. Sorry haven't updated with the latest news.

    So the car was on the dyno in May and made 15hp and 20lb-ft less. Even with the Cobb intake. After talking with Maine, the turbo was most likely culprit. So it was back to Andrewtech.

    Well some how the wategate flapper wasn't tight and was opening early with little pressure. So turbo off to disassemble and reassemble properly. While it was there I had a Crawford air/oil separator installed.

    Haven't had it back on the dyno since but I'm glad the wastegate issue was resolved and the separator. It drives a little bit more 'turboish' I think. I'll do what I can to get an in car vid soon.

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