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Taropatch

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Posts posted by Taropatch

  1. Hello all, I am having trouble finding the cause of my current issue.

    I rebuilt my 05 OBXT last summer and had an uneventful break-in period. I then began tuning the car with the guys over at cryo and without making that much power we were maxing out the MAF on the stock air box. I thought this was strange because almost every post I have read on the forum states that the stock air box is capable of 300ish hp. The logs were not putting up much more than stock boost. Fast forward and I changed the air box to the Cobb intake with enclosure and now were back with the same issue just with more boost and it has begun to lean out at the high end causing knock. I have double check all connections, smoke tested it, and it looks to be getting good vacuum numbers so I don't think it has anything to do with that.  I installed a new MAF during the rebuild and have cleaned it a few times since with out any change. I have zero issues with normal driving, but generally keep it out of boost.  

     

    To summarize current issues are: 

    1. MAF sensor maxing out  (looking at the tune it has been scaled up 13%)

     2. leaning out at higher RPM 

    3. and the knock around 3800

     

     

    Here is the short list of relevant mods:

    RA short block

    Rebuilt stock B25 heads

    all new vacuum lines and in bay fuel lines 

    new in tank fuel filter 

     

    Fuel:

    DW 750cc injectors 

    Tomei FPR set to 3 bar

    DW 65c pump

     

    intake: 

    stock manifold with phenolic spacers 

    and TGV flap delete 

    Grimmspeed top mount intercooler 

    Kinugawa 16g  

    Mishimoto turbo inlet 

    Cobb intake 

    Grimmspeed BCS

    Exhaust:

    Stock headers with Grimmspeed cross over 

    some aftermarket catless uppipe

    Grimmspeed down pipe 

    and custom catback exhaust 

     

    Here is the last log after I made sure everything was tight. I probably wont make another pull until I find an issue.

    Any help is appreciated!

     

     

    R2 3rd gear pull after fix.xlsx

  2. Hey all I have been having an issue with my OBXT surging when cruising. It happens in all gears. Usually around 3k rpm its most noticeable and only if I am holding the throttle in one spot.

     

    The engine is stock except DW65c pump and Tomei FPR (added after the issues began, thinking it was fuel related)

    Competition clutch "stock" replacement with SMFW.

     

    LGT suspension geometry conversion and full refresh of bushings and coils front to back.

     

     

    Today I did some logging and during a cruise the AFR is fluctuating from 11-18 without any change in throttle input. In a 3rd gear pull its leaning out to 20.33 and now it's parked until I can figure it out. I was thinking maybe a post MAF leak but couldn't find any yet.

     

    Anybody have issues with this before? I have been unable to find a thread addressing this.

     

     

     

     

     

    here are the logs:

    Cruising: https://docs.google.com/spreadsheets/d/1vZstxaAro40Ks2ZI1yxb_RbfNPZj7JDDdKR2l56qdic/edit?usp=sharing

     

    3rd gear pull:

    https://docs.google.com/spreadsheets/d/1Ct4bmL7FL9L9UlofDehYj4SR_UGC5uRUp7SHNnrCbBk/edit?usp=sharing

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