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trevorno

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Posts posted by trevorno

  1. I get a shuddering sound and vibration when turning the steering wheel. It happens when I'm stationary or moving. I replaced the return hose o-ring already, which helped with the ps whining sound, but I still get this shudder/slight vibration. Plenty of fluid and I've done a couple of locked turns in either direction.  I've just ordered a new return hose.

    The car is an 09 Legacy AT with 140K miles. I bought it 1.5 years ago. 

    What should I look at?

  2. I took the SS on a little 300 mile road trip. It's a fun cruiser and performed flawlessly. AC compressor doesn't work at all now and it was 95 out but not too hot with the windows rolled down.

     

    Trevorno, sorry to hear you had to sell it. 20 year old cars can be a constant pain.

     

    Thanks Monkey. Lesson learned not to buy a non running car sitting for 9 years. One thing after another. The wife was the happiest to see it go.

  3. Found oil puddling on top of the passenger side of the block. I had my SS for sale at the time. A self proclaimed "subaru guy" showed up and declared the block had cracked... HUH! He then said he could make me an offer. No thanks. I did some research on BBS and thought I'd try re-sealing the oil pressure sensor. I pulled the alternator off and teflon taped the threads on the sensor. I then saw the crankcase breather hose had become loose on the fitting on the block. It was still somewhat attached but the hose end had stretched and didn't fit tight. It was pointing toward my new oil puddle. I put a new hose on it with a screw down clamp for good measure. I degreased everything and sprayed off the engine at the car wash. Now to drive it for a bit and make sure my puddle doesnt reappear. Also need to head to the junkyard for a new hood latch and some interior trim pieces.
  4. I fixed a coolant leak to the turbo by using hose clamps instead of the spring clips. I also cleaned the MAF and found the glue I used to attach one of the plastic nipples to the air box had come loose and had a leak. I was pinched for time, so I used some 5 min epoxy to put it back together. I need to gather some courage and do the coffee cup mod.

     

    I went to the Junkyard and got some extra screws for the air box. I epoxied one of the nuts in place to the back of it. I also discovered the earlier mentioned nipple fix had failed so I tried it again with more epoxy. I also found some bolts to secure the bottom of the back seat and screws for my license plates.

  5. So, the cam was seized in the bolt-on collar on the front of the head. I pulled it off, took it back to the machine shop, where it was re-honed and liberally lubed before installation. Got it back on and started the car. Drove it about 10 miles before it seized again. Not in the collar this time, but somewhere in the head itself. I can turn it very slowly, but something is jammed up. So back it goes. Wondering if I need a new cam altogether?

     

    It also ripped the cogged roller out of the water pump and chewed the timing belt. Good times.

  6. I superglued the plastic nipple back on the purge valve, same treatment to the nipple on the large airbox between the filter box and the manifold. Looks like it's holding so far. Got everything back together and fired it up! Ran great for 10 seconds before it banged to a stop. Sounds like the timing belt slipped. I turned the crank with a wrench and could feel the teeth on the crankshaft hopping over the belt. I'll try to pull it apart tomorrow and see what's what. I hope my newly rebuilt heads havent seized.
  7. Pulled the motor from the '94 SS today. I ended up tearing apart the exhaust heat shield on the driver's side like an old tin can. The bolts were all rusted and fused together. My brother in law was helping me and discovered when I put the timing belt on, I had left the pin in the tensioner. I've only driven about 300 miles, but lucky for me I guess. I pulled the heads off and found a little bit of milky in the risidual oil left in the block. A lot of corrosion on the head bolts too. There was a ton of oozed oil on the back of the motor from the separator plate. Kind of a pain to tackle it all, but it'll be worth it when its done.
  8. anyone know why someone would disconnect the hill holder? I was cruzin down the block one day when all of a sudden no go?? popped the hood at the light and noticed it wasnt connected turned it the other way and drove away. tied it off with some tie wire and it seems to be fine. looks like everything is there but disconnected.why why why??

     

    Some of us appreciate the challenge of using a clutch and right foot braking like real men... Just kidding. I ended up leaving mine disconnected after I put my motor in. The hours spent getting my clutch cable threaded and re-connected relieved me of all my patience and ability to work in cramped spaces. That, and I am a real man...:)

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