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Grumblerton

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Posts posted by Grumblerton

  1. I'll be removing them tomorrow after work and resetting the ECU. It definitely seems like the inner flaps were causing some boost issues. Driving today the AP was reading 16.5 PSI peak which is only a half pound below target. Still some stumbling present. I'll see how it works tomorrow and if still no luck I'll have to order a new coupler. Any suggestions?. A quick search only showed cobb, perrin, and avo options. Nothing generic seemed to pop up.
  2. So update, drove home with the 93 map. Not a single problem at all. Got home and had the car idling while I loaded it for a trip to the house I recently bought. Issue started again after leaving. I’m going to try and look through all the vac lines and especially any of the intake piping this weekend. Just taking it easy on the car from now until I can get it on ramps and look underneath. Could it be a turbo issue or a bpv issue as well? I’m seriously at a loss of what could be causing it. Today’s temps were 42 at 5:30 am and 65 at 3:00 pm. I’m in southeast PA.
  3. So quick update while I’m on break at work. Reflashed the ECU this morning with the original 93 map and the stutter was less pronounced. I’m going to try the 91 map on the drive home and see what happens. I can try and get a couple good data logs comparing what the car is doing between 91, 93, and maybe even stock. No CEL or even a flashing CEL during the stumbling. MAF will be pulled and cleaned thoroughly again. Did a preliminary look at the vacuum lines I could see and everything seemed secure and still flexible. Could it be plugs? Still not hitting target boost of 17 psi and averaging around 15.6-16.4 peak. I looked at the intake and the charge pipe boots and saw no cracks and everything was butted up to the metal end fully.
  4. I recently got gas but it has been a consistent problem through 2 tanks but I have filled up from the same chain at stores within a couple miles of each other. I'll try stepping back to a 91 tune and seeing if that might be the problem. Something tells me I might have gotten some bad gas. MAF will get pulled and cleaned tomorrow. Thanks a ton so far, hopefully I'll have good news to report.
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